My self ported 760 mutt has been ripping in my Rickter for 4 years now. It started to develop some strange noises a few months ago but was still pulling hard and pushing solid compression. I decided to do a full tear down along with a returf.
One of the wrist pin bearings fell apart when I pushed out the pin and the middle lower crank bearings had been puking their guts out which somehow was retained inside the bearings.
Overall, I think I caught it moments before it totally came apart. Not bad for a bare bones budget build with all the cheapest parts running 190psi on zeel with 89 octane fuel.
One of the wrist pin bearings fell apart when I pushed out the pin and the middle lower crank bearings had been puking their guts out which somehow was retained inside the bearings.
Overall, I think I caught it moments before it totally came apart. Not bad for a bare bones budget build with all the cheapest parts running 190psi on zeel with 89 octane fuel.
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