I feel like a wide band o2 would be extremely helpful if it gave meaningful readings, for developing the base map, probably tune 0-100% throttle tied to a trailer in the water, cruising down the lake and out of water(won’t hit 100% here) and interpolate between those three lines to fill in your base fuel map, then I think you have to take it out and tune accel enrichment by riding it. I had not heard of x-tau enrichment but it sounds great, I think for a two stoke you will end up with a large x and long tau because fuel isn’t just stuck on the intake port wall, it has the whole crankcase and transfer port area to stick to. I didn’t get that deep into it but I’m hoping the mega squirt can just correlate throttle position to a map at a certain rpm(I think that’s how it handles alpha-n to begin with) and then derive mapdot from that for faster response.
I did message @tyler breitweser but he didn't offer up too much info
lol, well its in so I'll try it I guess. Although may be moving this project over to an eme hull thanks to my local used hull dealer @Rushford_Ripper and the amp will sit for a while longer, space may be a concern in the eme though hopefully I'll get some time to work on it this week or nextSo, I did exactly what you did with the drive shaft. My boss at the time, a self made machinist, told me it would not work. Mark Ericson told me it would not work unless perfectly balanced. And still probably not. I had it trued to less than .001 of runout. It broke in less than 2 hours of riding. Trying to save you the hassle.
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I rode it in the rickter for a grand total of about 10 min. Started way to rich on the jetting, leaned it out on the trailer before ever hitting water, hit the water for a couple min was still too rich took it home and rejetted, took it out again putting around not going too crazy to break it in. It shot right out of the water the few times I whacked the throttle like it never had with the 701 based setup. Problem was I used pretty thin cooling line from mcmaster that ended up melting off pretty quickly, so overheated the motor and sprayed water everwhere, ski started to loose power, I limped it back to the launch. Pulled the heads to see if I melted those o rings too and found that some metal also bounced around between the piston and head. I had bought a 62t 850 already and it had come in and was sitting in a box next to all the parts I had just ripped out of the rickter. So back in all that went so I could ride it some last summer and I still have yet to tear into the 66e to see what all happened. Hoping the plating is still good and I can slap it in something before this summer.Did you get to ride this thing?