- Location
- Fenton, Michigan
Let's go back 2 years ago when my dual carb 701 ran well. Mods are B pipe (limited), 93 octane girdled head, blowsion flame arrestors, 9/15 hooker, dual cooled. Jetting was 130 Main and 75 pilot 95g spring. I never checked the needle and seat or pop off. It ran great until it didn't.
Carbs are sbn38s with the t screws added.
I then bought complete mikuni rebuild kits and went through the carbs thoroughly. Rebuild and test on her again. Bogging low and high. Mid range is ok. Adjusting the low end I was able to get it close but the high side was garbage. I even went up a main and down a main size with the same result. I chased this with this for almost a year with different jet combos.
Fast forward to this year. My buddy has a similar build SJ so we swap carbs. Mine came back to life with his which has the same jetting. I buy the revised version of the sbn38s with the t screws already installed. I have a 1.5 N&S 65g spring 135M 75P. 28 psi pop off.
Played with 1 size up and down on the main and pilot and still have issues at mid to high end (plugs are reading perfect to slightly rich).
I installed a linkage kit today because I noticed as one butterfly opens, there was some lash causing a slight delay before the other side would open and I was hoping that was it as the linkage kit made a solid synced connection.
Anyone have any other ideas??
Carbs are sbn38s with the t screws added.
I then bought complete mikuni rebuild kits and went through the carbs thoroughly. Rebuild and test on her again. Bogging low and high. Mid range is ok. Adjusting the low end I was able to get it close but the high side was garbage. I even went up a main and down a main size with the same result. I chased this with this for almost a year with different jet combos.
Fast forward to this year. My buddy has a similar build SJ so we swap carbs. Mine came back to life with his which has the same jetting. I buy the revised version of the sbn38s with the t screws already installed. I have a 1.5 N&S 65g spring 135M 75P. 28 psi pop off.
Played with 1 size up and down on the main and pilot and still have issues at mid to high end (plugs are reading perfect to slightly rich).
I installed a linkage kit today because I noticed as one butterfly opens, there was some lash causing a slight delay before the other side would open and I was hoping that was it as the linkage kit made a solid synced connection.
Anyone have any other ideas??