I picked up a 91 650sx with many extra parts for cheap, I was told it had an air leak. The ski was pretty rough, but it fired right up every time I tried, so I took it out for a little ride and found that they guy had the throttle cable adjusted way to tight. (his "air leak"). He had obviously tried to adjust the carbs in order to get it to dial back (I got maybe 1/4 throttle out of it and the screw caps where chewed up bad)
So I adjusted them back to the stock settings and though I got better response and higher revs it still didn't rev past maybe 3/8 throttle. So after more fiddling with the screws and blowing apart the exhaust(loud bang, scared the hell out of me. Shut it down, and found it blew apart at the boot)
I decided I was going to order a rebuild kit among other things. So now I have a carb rebuild kit on the way, a proper throttle lever to replace the bicycle brake lever that didn't give full throttle, a full Gasket set, fuel line and clamps, new plugs and boots (I have 2 coils and 1 the wires are to short to mount it properly but the other doesn't have boots) and will be properly mounting the electronics. Also in the order are a bunch of waterproof bullet connectors to replace the corroded ones that are in this e box.
It also didn't want to suck any water out. Today I found the bailer tube wasn't attached in the hull, and the screen was clogged solid.
Now I question whether this is even the right e box as it doesn't seem to mount anywhere properly. Any ideas on this(see pictures)
I pulled the motor and gas tank today to clean out the hull and it wasn't good. Rust flakes and dust every where. Of course 3 of the 4 motor mounts broke so I'll have to do the fancy repair to all of them. I have wire wheeled the plate and sprayed it with self etching primer, and will be doing black engine enamel tomorrow. I'll finish cleaning the hull tomorrow and go from there.
So I adjusted them back to the stock settings and though I got better response and higher revs it still didn't rev past maybe 3/8 throttle. So after more fiddling with the screws and blowing apart the exhaust(loud bang, scared the hell out of me. Shut it down, and found it blew apart at the boot)
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It also didn't want to suck any water out. Today I found the bailer tube wasn't attached in the hull, and the screen was clogged solid.
Now I question whether this is even the right e box as it doesn't seem to mount anywhere properly. Any ideas on this(see pictures)
I pulled the motor and gas tank today to clean out the hull and it wasn't good. Rust flakes and dust every where. Of course 3 of the 4 motor mounts broke so I'll have to do the fancy repair to all of them. I have wire wheeled the plate and sprayed it with self etching primer, and will be doing black engine enamel tomorrow. I'll finish cleaning the hull tomorrow and go from there.