- Location
- Seattle
So I recently purchased a rebuilt motor with a 61x crank and cylinder and an 62 t head from SBT. When putting it in i replaced the fuel lines, rebuilt the carbs (dual 38) I just got a new factory b limited and it has carbon fiber reeds and dual exhaust. Nothing too fancy. On my 1st test run I was having a Pretty bad issue with bogging After quarter throttle The for I got to wide-open throttle but I was able to feather it through the mid range to get to wide-open throttle if I did it just right . So I took it out of the water and Came to the conclusion that it was running rich so I put bigger pilot and main jets in Factory pipe recommended a 135 in a 70 to start with so after the boggish you I put a 140 mean and a 70 pilot. This did pretty much nothing. It then turned into an investigation taking the carbs off 3 more times To Go down to half sizes of jets in then adjust pop off pressure from 55PSI down to 30PSI. Here's where it gets exciting I finally got great results from lowering the pop off pressure significantly So I put it in the water and went for a ride in the road very well with only a very very minimal amount of bog on the bottom-end. Then I was at quarter throttle for a long period and it started To feel like it was running on one cylinder like I had fouled a spark plug. I then changed the plugs and had the same slow sluggish ski. Then changed the coil.... same slow ski. I'm starting to think that it must be some kind of electrical issue because I finally got Running with Virtually no bargaining at all-and then all the sudden the symptoms significantly changed when I went for that one ride. I'm really hoping you guys can put your heads together and see if you can come-up with something else for me to try because I'm quite literally a dead and and have no idea what else to do with this money pit that I love so much lol . Let me know if you want pics or more info. I tried to be thorough but I know I'm not very descriptive