I finally got my Blaster on the water! I have been out with an injury and have waiting months to try this thing out! The last time I rode, it was completely stock. I was able to collect a good list of parts at a good price, with the help of several members on here (Thanks guys!). My goal was to boost performance a little without ending my marriage. (So far so good)
Blaster list of mods:
Wetjet 46mm SBN carburetor
Wetjet reed stuffer manifold
Boysean two stage reeds
Oceanpro Vortex flame arrestor
Primer/choke plate eliminated
Protec half girdle
Wetjet/Westcoast with 30cc domes (180psi)
Wetjet/Westcoast pipe (everything has been shaped to match the exhaust gasket)
TDR waterbox
Skat-trak 12-17 big hub prop, 3mm set back
Protec open intake grate
R&D ride plate...
So I get it backed into the water and idle it for a little while to get the low screw and idle set. Everything looked good. Cooling system was working and no there was no flames or explosion, great! I get it out on the water and accelerate away from the shore. I am amazed at the difference! I didn't recognize my ski! It was fun stock, but it's a monster now! It's hard to explain how snappy the throttle is and how hard it pulls! All was well then I noticed my newly installed pisser stopped flowing (probably bad) and I shut it down immediately. I completed my cardio for the day with a nice little swim. Luckily I shut it down because I found the cooling line to the head had popped off. A new hose clamp and I was good to go! I sure am glad I installed that pisser because this would have been a depressing thread.
I need to get a tach on this thing so I can really tune it right. The old Butt Dyno said I'm close. At the end of the day I noticed my fuel pump was leaking and I could not stop it by tightening the bolts. I put the Blaster back on the trailer and continued riding my old WaveJammer (nothing like the Blaster but still one of my favorite skis!). I will pull it off and see why tomorrow.
Here is my rough game plan for jetting after yesterday's tests: I am going to bump my main jet up from a 155 to a 157.5 because the plug chop looked good but the high side was out nearly three turns. The low might stay at 130 because there was no lean hesitation. The transition was perfect so the pop off pressure is right on. Of course, I am going to deal with the leak prior to changing anything. I don't think it was leaking during the tests but I cannot be sure.
All I can say is my ski is on the right track! The motor makes ridiculous power compared to stock. The new impellor is amazing as well. I feel NO cavitation at all. You hit the throttle and it jumps out of the water! The ski feels better in all ways!
I just wanted to give everyone an update my project and thank you for your help!
Blaster list of mods:
Wetjet 46mm SBN carburetor
Wetjet reed stuffer manifold
Boysean two stage reeds
Oceanpro Vortex flame arrestor
Primer/choke plate eliminated
Protec half girdle
Wetjet/Westcoast with 30cc domes (180psi)
Wetjet/Westcoast pipe (everything has been shaped to match the exhaust gasket)
TDR waterbox
Skat-trak 12-17 big hub prop, 3mm set back
Protec open intake grate
R&D ride plate...
So I get it backed into the water and idle it for a little while to get the low screw and idle set. Everything looked good. Cooling system was working and no there was no flames or explosion, great! I get it out on the water and accelerate away from the shore. I am amazed at the difference! I didn't recognize my ski! It was fun stock, but it's a monster now! It's hard to explain how snappy the throttle is and how hard it pulls! All was well then I noticed my newly installed pisser stopped flowing (probably bad) and I shut it down immediately. I completed my cardio for the day with a nice little swim. Luckily I shut it down because I found the cooling line to the head had popped off. A new hose clamp and I was good to go! I sure am glad I installed that pisser because this would have been a depressing thread.
I need to get a tach on this thing so I can really tune it right. The old Butt Dyno said I'm close. At the end of the day I noticed my fuel pump was leaking and I could not stop it by tightening the bolts. I put the Blaster back on the trailer and continued riding my old WaveJammer (nothing like the Blaster but still one of my favorite skis!). I will pull it off and see why tomorrow.
Here is my rough game plan for jetting after yesterday's tests: I am going to bump my main jet up from a 155 to a 157.5 because the plug chop looked good but the high side was out nearly three turns. The low might stay at 130 because there was no lean hesitation. The transition was perfect so the pop off pressure is right on. Of course, I am going to deal with the leak prior to changing anything. I don't think it was leaking during the tests but I cannot be sure.
All I can say is my ski is on the right track! The motor makes ridiculous power compared to stock. The new impellor is amazing as well. I feel NO cavitation at all. You hit the throttle and it jumps out of the water! The ski feels better in all ways!
I just wanted to give everyone an update my project and thank you for your help!