- Location
- New Jersey
Is water getting into the engine? When is boggs, pull the plugs and see if there is any chocolate milk inside.
Any unusual flow out the pissers you've noticed spitting and what not ?
So it all started after the water box failure and repair or new cooling routing? If that's true your ski ran fine prior in the bigger wakes you've mentioned?
Have you had a chance to inspect the box internally for loose intermittent blockages?
I haven't.
Also what about removing your head pipe and putting it on the water hose to verify your spray and no odd sprays/cracks
How is it adjusted, won't cause your issue but are you closed bottom and middle and open 3/4 top?
Bottom cracked just so it lightly sizzles after WOT. Recommended by Zack at PHP, and it has an awesome powerband with this setup.
How much compression does it have now
I have no idea. It had 180 the last time I checked it(over a month ago)
What's the deal with water pressure, pull out those restricters you have and see if any changes occurs
Restricter is used to get enough pressure to the headpipe. Typical dual cooling- 2 lines into mani, rear cylinder outlet to pisser, front to bottom of headpipe, top of headpipe to a tee. Straight part of tee to a FCV, then to stinger. Angled part to a pisser with a restriction.
You'll prolly have to only put a gallon of fuel in after you completely drain it and see if the low fuel/fuel level is at play or just a coincidence
It could very well be fuel or ignition/electrics like you mentioned
A little more info I guess, but I've thought it irrelevent since it was running so good on flatwater...I found my waterbox messed up because I had to replace my stator- was adjusting rpms with a tach on a riva cdi that I was putting in, and my starter relay slipped and grounded out on the ebox, completely frying the ground wire off the stator. Needless to say I got a used stator, and used my modded protec CDI instead. I don't know if it took a tole on my coil, since this doesn't seem like normal bad coil symptoms. Like I said, it ran nearly perfect on flatwater after I replaced the new stator.
Carb was rebuilt by me with genuine mikuni parts. Everything's been working great for 70ish hours. Lines are 3/16 tygon(new line this year), so it's a super snug fit to get them on the fittings, and then ziptied. I've seen people not even use anything to hold 3/16 tubing on since it's a snug fit.
The return is not drilled out as it's just a stock 44mm SBN that came on my 95 square.
Thank you for that awesome response propulsion..I really appreciate it! Got me thinking now.
It makes me wonder if somehow the shortage messed with the coil..Otherwise it could possibly be a fuel issue..it's just super wierd haha. Wanna get this figured out before the lakes freeze over. Planning on sportporting my cylinder, but I'd like to have it running right before I start messing with it again.For me this type of information is critical, before this it was good and after this incident/repair it's bad, it helps narrow the field down