As for roseand's issue: A single 44 should be easier to tune
but my guess is needle and seat is too small or popoff is too high and you were running lean at that 2/3-3/4 mark you feel is "safer" to not blow your engine. You probably would have been safer at WOT with that 150 main in there than the cruising speed.
plus im betting the piston to wall clearance was too tight for the mods done
although he not believing it because it ran last season like that-don't rule out some of the things i pointed out
ported engine will run different piston and egt's temperatures